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Ferrosilicon

Application

Filter evacuates an electric arc furnace used to produce 1416% FeSi

Optimization Potential

Baghouse airflow was 30% below design. This caused insufficient heat removal at the furnace. Maintenance of electrode system and mechanical stokers increased. Holes were cut in the ducting after the furnace to draw in cool air, as the aramid fiber bags used could only be operated up to 190oC. Aramid fiber bags failed after 12 to 18 months due to hydrolysis caused by steam that passed through the baghouse when leaks occured in the furnace cooling water supply.

Solution

Installed GORETM  membrane filter bags with Teflon B® woven glass backing material and new cages. Optimized system flow settings.

Results

Extraction at the furnace has increased above the design. The main fan damper is partially closed to control the extraction at the furnace. Tapping fume has been added into the same baghouse. The smelt house environment is much cooler, and it led to a decrease in maintenance of the electrode system and mechanical stokers. The GORE Membrane/Teflon B glass bags lasted 3 years and were immune to hydrolysis. The operating temperature has been increased to 230oC. Visible emission at the stack has been eliminated. After 3 years, the first set of GORE membrane filter bags were replaced with SUPERFLEX® filter bags which have now been in operation for more than 5 years. The electrical capacity of the furnace has been upgraded by 30%.

Ferrosilicon (122 KB  )


 

 


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